Autonomous Submarine Project: Part 4

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Autonomous Submarine Project: Part 4

Sep 10, 2018

Michael Denny


More bench testing was done, I found out that the motor needs to be mounted perfectly straight to be strong enough to turn the shaft. So now a new holder was designed and is being printed. To mount the motor straight and tight to stop it from sliding back during assembly I will be using the screws from the two broken motors. A hole was also made at the top off the hull for the magnet to go through and start the sub.

 

autonomous submarine

 

autonomous submarine